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Accession Number:

AD1183314

Title:

T-46A Flight Test Reports Jan - Mar 87

Author(s):

Author Organization(s):

Report Date:

2022-10-25

Abstract:

Air abort due to instrumentation parameter 742 inoperative. No flight test data obtained. On the ground, gusty wind conditions caused fluctuations in the H1 engine (RPM, EGT, fuel flow) which were elimated by selecting manual fuel control. The #2 engine, which has the 110D record 6 ECU, operated normally.

Pages:

98

File Size:

12.46MB

Descriptors:

Identifiers:

Distribution Statement:

Approved For Public Release

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