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Accession Number:
AD0880628
Title:
Flexible Exit Cone Nozzle Firing.
Corporate Author:
AIR FORCE ROCKET PROPULSION LAB EDWARDS AFB CA
Report Date:
1970-12-01
Abstract:
This report describes the test firing of a thrust vector control TVC system on the AFRPL 40-inch-diameter char motor. The TVC system developed under Contract F04611-68-C-0004 consisted of a movable exit cone Flex-X nozzle and support hardware, which was designed to combine the advantages of the elastomeric bearing with those of the supersonic splitline nozzle. The elastomeric bearing failed after 21 seconds of motor operation. Probable reasons for the failure and a general description of the preparations and motor performance are described in the text. Author
Descriptive Note:
Technical rept.,
Pages:
0040
File Size:
0.00MB