Accession Number:

AD0442858

Title:

X-22A TRI-SERVICE V/STOL AIRCRAFT

Personal Author(s):

Corporate Author:

BELL AEROSYSTEMS CO BUFFALO NY

Report Date:

1963-10-01

Abstract:

Designs and release of drawings to manufacturing for fabrication of parts is progressing. Weight Control effort has been maintained, and changes in the target weight are fluctuating with the release of detail design and due to many adjustments resulting from subcontracted systems and changes authorized by Cockpit Mockup Inspection. All changes resulting from Cockpit Mockup Inspection are presently being packaged for formal submittal to BuWeps. Reduction of wind tunnel data from the 15 scale, 17 scale, and ground effects models progressed. Test preparations for continued wind tunnel model tests were made. The Acoustic Noise Test of the fuselage test specimen as well as the Salt Spray tests and Low cycle-high stress fatigue tests of maraging steel specimens were all completed.

Descriptive Note:

Monthly progress rept. no. 11, 1-31 Oct 1963

Pages:

0055

Subject Categories:

Communities Of Interest:

Modernization Areas:

Distribution Statement:

Approved for public release; distribution is unlimited.

Contract Number:

NOW-63-0118-CI

File Size:

5.58MB